It is well-known that the better the control of the liquid aluminium allows obtaining of better properties. One of the most important defects that is held responsible for lower properties has been the presence of porosity. Porosity has always been associated with the amount of dissolved hydrogen in the liquid. However, it was shown that hydrogen was not the major source but only a contributor the porosity. The most important defect that causes porosity is the presence of bifilms. These defects are surface entrained mainly due to turbulence and uncontrolled melt transfer. In this work, a cylindrical mould was designed (Ø30 x 300 mm) both from sand and die. Moulds were produced both from sand and die. Water cooled copper chill was placed at the bottom of the mould in order to generate a directional solidification. After the melt was prepared, prior to casting of the DC cast samples, reduced pressure test sample was taken to measure the melt quality (i.e. bifilm index). The cast parts were then sectioned into regions and longitudinal and transverse areas were investigated metallographically. Pore size, shape and distribution was measured by image analysis. The formation of porosity was evaluated by means of bifilm content, size and distribution in A356 alloy.
A356 is one of the widely used aluminium casting alloy that has been used in both sand and die casting processes. Large amounts of scrap metal can be generated from the runner systems and feeders. In addition, chips are generated in the machined parts. The surface area with regard to weight of chips is so high that it makes these scraps difficult to melt. Although there are several techniques evolved to remedy this problem, yet the problem lies in the quality of the recycled raw material. Since recycling of these scrap is quite important due to the advantages like energy saving and cost reduction in the final product, in this work, the recycling efficiency and casting quality were investigated. Three types of charges were prepared for casting: %100 primary ingot, %100 scrap aluminium and fifty-fifty scrap aluminium and primary ingot mixture were used. Melt quality was determined by calculating bifilm index by using reduced pressure test. Tensile test samples were produced by casting both from sand and die moulds. Relationship between bifilm index and tensile strength were determined as an indication of correlation of melt quality. It was found that untreated chips decrease the casting quality significantly. Therefore, prior to charging the chips into the furnace for melting, a series of cleaning processes has to be used in order to achieve good quality products.
The formation of oxide film on the surface of aluminium melts, i.e. bifilms, are known to be detrimental when they are incorporated into the cast part. These defects causes premature fractures under stress, or aid porosity formation. In this work, Al-12 Si alloy was used to cast a step mould under two conditions: as-received and degassed. In addition, 10 ppi filters were used in the mould in order to prevent bifilm intrusion into the cast part. Reduced pressure test samples were collected for bifilm index measurements. Samples were machined into standard bars for tensile testing. It was found that there was a good agreement with the bifilm index and mechanical properties.
In the present study, the corrosion behaviour of A356 (Al-7Si-0.3Mg) alloy in 3.5% NaCl solution has been evaluated using cyclic/potentiodynamic polarization tests. The alloy was provided in the unmodified form and it was then modified with AlTi5B1 for grain refinement and with AlSr15 for Si modifications. These modifications yield to better mechanical properties. Tensile tests were performed. In addition, bifilm index and SDAS values were calculated and microstructure of the samples was investigated. As a result of the corrosion test, the Ecorr values for all conditions were determined approximately equal, and the samples were pitted rapidly. The degassing of the melt decreased the bifilm index (i.e. higher melt quality) and thereby the corrosion resistance was increased. The lowest corrosion rate was founded at degassing and as-received condition (3.9x10-3 mm/year). However, additive elements do not show the effect which degassing process shows.