Turbine blades have complex geometries with free form surface. Blades have different thickness at the trailing and leading edges as well as sharp bends at the chord-tip shroud junction and sharp fins at the tip shroud. In investment casting of blades, shrinkage at the tip-shroud and cord junction is a common casting problem. Because of high temperature applications, grain structure is also critical in these castings in order to avoid creep. The aim of this work is to evaluate the effect of different process parameters, such as, shell thickness, insulation and casting temperature on shrinkage porosity and grain size. The test geometry used in this study was a thin-walled air-foil structure which is representative of a typical hot-gas-path rotating turbine component. It was observed that, in thin sections, increased shell thickness helps to increase the feeding distance and thus avoid interdendritic shrinkage. It was also observed that grain size is not significantly affected by shell thickness in thin sections. Slower cooling rate due to the added insulation and steeper thermal gradient at metal mold interface induced by the thicker shell not only helps to avoid shrinkage porosity but also increases fill-ability in thinner sections.
One of the most common reasons for horse lameness is subchondral bone cysts (SBCs), which are especially evident in young horse athletes. It is believed that SBC development is strongly associated with an individual’s bone growth and/or bone microstructure impairment. Current methods of SBC treatment include pharmacological treatment or surgical procedures which may allow the bone within the cyst to rebuild and be restored to properly developed bone tissue. Thus, we propose filling the SBCs with a 3D complex of alginate hydrogel and autologous adipose derived mesenchymal stem cells (ASCs). We have observed at the in vitro level, that this hydrogel complex induces osteogenic and chondrogenic differentiation potential through the upregulation of bone morphogenetic protein, osteopontin, collagen type I and aggrecan mRNA levels. Moreover, we detected the creation of a 3D extracellular matrix (EM). To investigate the complex in vivo, we chose 8 horses of varying age suffering from SBC, which resulted in lameness, to undergo experimental surgery. We documented the horses’ clinical appearance, lameness and radiographic appearance, to determine that there was clinical improvement in 87.75% of the patients (n=7, out of 8 horses) 6 months postoperatively and 100% (n=8, out of 8 horses) a year after surgery. These results are promising for the potential of this procedure to become the standard in SBC treatment.
Castability of thin-walled castings is sensitive to variation in casting parameters. The variation in casting parameters can lead to undesired casting conditions which result in defect formation. Variation in rejection rate due to casting defect from one batch to other is common problem in foundries and the cause of this variation usually remain unknown due to complexity of the process. In this work, variation in casting parameters resulting from human involvement in the process is investigated. Casting practices of different groups of casting operators were evaluated and resulting variations in casting parameters were discussed. The effect of these variations was evaluated by comparing the rejection statistics for each group. In order to minimize process variation, optimized casting practices were implemented by developing specific process instructions for the operators. The significance of variation in casting parameters in terms of their impact on foundry rejections was evaluated by comparing the number of rejected components before and after implementation of optimized casting practices. It was concluded that variation in casting parameters due to variation in casting practices of different groups has significant impact on casting quality. Variation in mould temperature, melt temperature and pouring rate due to variation in handling time and practice resulted in varying quality of component from one batch to other. By implementing the optimized casting instruction, both quality and process reliability were improved significantly.