Paper present a thermal analysis of laser heating and remelting of EN AC-48000 (EN AC-AlSi12CuNiMg) cast alloy used mainly for
casting pistons of internal combustion engines. Laser optics were arranged such that the impingement spot size on the material was a
circular with beam radius rb changes from 7 to 1500 m. The laser surface remelting was performed under argon flow. The resulting
temperature distribution, cooling rate distribution, temperature gradients and the depth of remelting are related to the laser power density
and scanning velocity. The formation of microstructure during solidification after laser surface remelting of tested alloy was explained.
Laser treatment of alloy tests were perform by changing the three parameters: the power of the laser beam, radius and crystallization rate.
The laser surface remelting needs the selection such selection of the parameters, which leads to a significant disintegration of the structure.
This method is able to increase surface hardness, for example in layered castings used for pistons in automotive engines.
In this study, low-carbon cast steel was reinforced with TiC by SHS-B method, also known as combustion synthesis during casting method. The composite zone was then subjected to surface remelting by Gas Tungsten Arc Welding (GTAW) method. The remelting operation was realized manually, at 150 A current magnitude. Microstructure, phase composition and hardness of remelted zone were investigated. XRD results reveal that the phases of the composite zone in initial state consist of TiC and Feα. Surface remelting resulted in formation of thick layers containing TiC carbides, Feα and Feγ. Microstructural examination has shown strong refinement of titanium carbides in remelted zone and complete dissolution of primary titanium carbides synthetized during casting. The average diameter of carbides was below 2 μm. The structural changes are induced by fast cooling which affects crystallization rate. The hardness (HV30) of the remelted layer was in the range between 250 HV and 425 HV, and was lower than hardness in initial state.